The Cothran valve has a 3/8" ID hole to hold the transfer port, but right at the bottom of that hole, it has a half-depth O-ring groove to retain a # 011 O-ring, that is nominally 5/16" ID x 7/16" OD.... This requires that the bottom 1/16" of the transfer port (it is intended that it be made from brass) is turned down to 5/16" OD.... I did that with my Teflon port, which for that bottom 1/16" left the wall thickness only 1/32", and it looks like that is what failed.... I thought about doing as you suggested, and leaving the Teflon 3/8" OD right to the bottom, but then the bottom 1/16" (maybe 0.070") would be unsupported because that area in the valve port recess has been removed to form the groove in the valve for the O-ring.... I was concerned that the TP would fail in that area, blowing outwards, or at the very least expand, locking the TP into the groove in the valve.... After examining the alternatives, I decided to use brass, and seal it at the top, against the barrel, with an 8mm x 10mm x 1mm Metric O-ring located in a shoulder in the top of the Transfer Port.... I made the brass transfer port with a 0.060" long shoulder (5/16" diam.) at the bottom, and a few thou long at the top, and then machined the length down until I could just push the receiver down against the main tube, by compressing the O-ring in the valve.... Being brass, the length is, of course, critical.... I then machined a shoulder 0.035" smaller in OD, and 0.035" deep, into the top end of the transfer port.... This puts the 1mm O-ring into significant compression.... I only tried a few shots, but it sealed perfectly, and I picked up 50 fps.... That makes me quite certain that the Teflon port started to fail almost as soon as I began testing at 2900 psi, which caused the velocity loss.... It is possible that it may have even affected the 1900 psi tests, that will be determined another day....In the meantime, I am pretty stoked to break 150 FPE at 2900 psi.... Bob